Total Complaints
2 filings
LEXUS ES · model year
2 NHTSA complaints for this specific cohort.
NHTSA overall rating
Not crash-tested
New Car Assessment Program
The 1996LEXUSES carries 2 consumer safety complaints in NHTSA's Office of Defects Investigation database for this specific model-year cohort. Within that volume, owners reported 0 crashes, 0 fires, 0 injuries, and 0 fatalities. No NCAP 5-star crash-test rating is available for this model year in the federal database.
Component-level analysis is where model-year complaints become actionable: the top complaint category for the 1996 ES is fuel/propulsion system with 1 filings, followed by engine (1). Concentration in one or two component groups is the classic signature of a systemic defect; a flat distribution usually reflects normal aging, warranty complaints, or isolated build-plant variability.
NHTSA currently has 3 investigation files overlapping the 1996 ES. Owners comparing this cohort against neighboring years should pair the counters above with the complaint-by-year trend on the parent model page — a spike in a single year often tracks to a platform refresh, a new transmission supplier, or an updated ECU calibration. Use the related-complaint feed below to read raw owner narratives before deciding whether any pattern here affects your specific use case.
Total Complaints
2 filings
Crashes Reported
0 reports
Source
NHTSA ODI
Federal complaints database
At or below the fleet median complaint volume.
| Component | Count |
|---|---|
| FUEL/PROPULSION SYSTEM | 1 |
| ENGINE | 1 |
I SMELLED WHAT I THOUGHT WAS TRANSMISSION FLUID OR ANTI-FREEZE. THE NEXT DAY MY WIFE SMELLED GAS AND SOME FRIENDS CALLED MY CELL TO TELL ME GAS WAS RUNNING OUT FROM UNDER THE CAR. I COULD NOT FIND A LEAK UNDER THE CAR. I LIFTED THE HOOD AND FOUND GAS RUNNING DOWN THE SIDE OF THE ENGINE. AFTER TAKING THE LEXUS COVER OFF THE ENGINE, I FOUND GAS SHOOTING STRAIGHT UP INTO THE AIR. IT WAS COMING FROM A VACUUM LINE THAT HAD POPPED OFF. I RE-ATTACHED THE LINE AND STARTED THE ENGINE. THE LINE POPPED OFF AND GAS AGAIN SHOT STRAIGHT INTO THE AIR. I REPLACED THE VACUUM LINE. IT STAYED ON BUT THE GAS RAN THROUGH A NEARBY SWITCH AND ONTO THE ENGINE. IT TOOK ME A WHILE TO FIGURE OUT THE GAS SHOULD NOT BE GOING THROUGH THE VACUUM LINE. THE FUEL PRESSURE REGULATOR HAD MAL FUNCTIONED AND ALLOWED THE GAS TO GO THROUGH THE VACUUM SIDE OF THE REGULATOR. WHILE DRIVING THE REGULATOR HAD ALLOWED OVER 10 GALLONS OF GAS TO POUR DIRECTLY OVER MY ENGINE. IT BOTHERS ME HOW EASY IT WOULD HAVE BEEN FOR THE CAR, MY
Mileage: 235,600
I SMELLED WHAT I THOUGHT WAS TRANSMISSION FLUID OR ANTI-FREEZE. THE NEXT DAY MY WIFE SMELLED GAS AND SOME FRIENDS CALLED MY CELL TO TELL ME GAS WAS RUNNING OUT FROM UNDER THE CAR. I COULD NOT FIND A LEAK UNDER THE CAR. I LIFTED THE HOOD AND FOUND GAS RUNNING DOWN THE SIDE OF THE ENGINE. AFTER TAKING THE LEXUS COVER OFF THE ENGINE, I FOUND GAS SHOOTING STRAIGHT UP INTO THE AIR. IT WAS COMING FROM A VACUUM LINE THAT HAD POPPED OFF. I RE-ATTACHED THE LINE AND STARTED THE ENGINE. THE LINE POPPED OFF AND GAS AGAIN SHOT STRAIGHT INTO THE AIR. I REPLACED THE VACUUM LINE. IT STAYED ON BUT THE GAS RAN THROUGH A NEARBY SWITCH AND ONTO THE ENGINE. IT TOOK ME A WHILE TO FIGURE OUT THE GAS SHOULD NOT BE GOING THROUGH THE VACUUM LINE. THE FUEL PRESSURE REGULATOR HAD MAL FUNCTIONED AND ALLOWED THE GAS TO GO THROUGH THE VACUUM SIDE OF THE REGULATOR. WHILE DRIVING THE REGULATOR HAD ALLOWED OVER 10 GALLONS OF GAS TO POUR DIRECTLY OVER MY ENGINE. IT BOTHERS ME HOW EASY IT WOULD HAVE BEEN FOR THE CAR, MY
Mileage: 235,600
Data as of 2025. Sources: NHTSA Office of Defects Investigation (ODI) complaints database, NHTSA recall campaign API, NHTSA NCAP crash-test ratings, and NHTSA FARS for fatality cross-reference.
Read our methodology — how this data is sourced, computed, and verified.