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2013 FORD EXPEDITION — Complaint #1857924

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NHTSA Complaint about VISIBILITY:DEFROSTER/DEFOGGER/HVAC SYSTEM:FAN/MOTOR:RESISTOR/SPEED CONTROL filed December 7, 2022

NHTSA complaint #1857924 (ODI reference 11496423) concerns a 2013 FORD EXPEDITION and was filed on December 7, 2022. The owner reports the failure occurred on December 6, 2022. The vehicle had 134,000 miles on the odometer at the time of the incident. The report was geocoded to Minnesota based on the filer's self-reported location. The affected component is categorized as visibility:defroster/defogger/hvac system:fan/motor:resistor/speed control, one of NHTSA's standardized taxonomy codes used to group defect patterns across make, model, and year.

The filer flagged the following severity indicators: crash: no, fire: no, injuries: 0, fatalities: 0. No crash, fire, or fatality was associated with this report, which places it in the early-warning stream rather than the priority-review stream. Because a VIN was supplied, this complaint is tied to a specific vehicle and not just a model-year cohort.

Individual complaints are consumer-submitted and unverified by NHTSA engineers — the agency's role at this stage is to collect, index, and make them searchable. What matters for federal action is the pattern: when many owners of the same FORD EXPEDITION cohort independently describe similar visibility:defroster/defogger/hvac system:fan/motor:resistor/speed control failures, defect investigators have grounds to open a PE and request manufacturer data. Related filings for the same vehicle and component appear below, and the detail page for the full 2013 FORD EXPEDITION shows the complete component-level complaint distribution alongside any active investigations or recalls.

Vehicle
2013 FORD EXPEDITION
Component
VISIBILITY:DEFROSTER/DEFOGGER/HVAC SYSTEM:FAN/MOTOR:RESISTOR/SPEED CONTROL
State
Minnesota
Mileage
134,000 mi

Complaint Description

The contact owns a 2013 Ford Expedition. The contact stated that when she attempted to operate the heating system, she heard a loud whistling sound and knob became stuck on high speed. No warning light was illuminated. The vehicle was taken to an independent mechanic where it was diagnosed that the blower motor controller and connector had burned and needed to be replaced. The vehicle was repaired; however, the failure recurred. The vehicle was taken back to the independent mechanic where it was diagnosed that the blower motor controller and connector needed to be replaced. The vehicle was repaired. The manufacturer was notified of the failure and the contact was informed that the VIN was not included in a recall and to call the NHTSA Hotline for assistance. The failure mileage was approximately 134,000.

Complaint Details

NHTSA Complaint ID 1857924
ODI Number 11496423
Date Filed December 7, 2022
Failure Date December 6, 2022
VIN 1FMJU2A59DE

Source: NHTSA Vehicle Complaints Database. Component taxonomy and severity codes are standardized by NHTSA Office of Defects Investigation.