2017 FORD ESCAPE — Complaint #1780905
Open-data reference.
NHTSA Complaint about ENGINE AND ENGINE COOLING:ENGINE:OIL/LUBRICATION: OIL COOLER filed November 30, 2021
NHTSA complaint #1780905 (ODI reference 11442144) concerns a 2017 FORD ESCAPE and was filed on November 30, 2021. The owner reports the failure occurred on November 10, 2021. The vehicle had 107,000 miles on the odometer at the time of the incident. The report was geocoded to Florida based on the filer's self-reported location. The affected component is categorized as engine and engine cooling:engine:oil/lubrication: oil cooler, one of NHTSA's standardized taxonomy codes used to group defect patterns across make, model, and year.
The filer flagged the following severity indicators: crash: no, fire: no, injuries: 0, fatalities: 0. No crash, fire, or fatality was associated with this report, which places it in the early-warning stream rather than the priority-review stream. Because a VIN was supplied, this complaint is tied to a specific vehicle and not just a model-year cohort.
Individual complaints are consumer-submitted and unverified by NHTSA engineers — the agency's role at this stage is to collect, index, and make them searchable. What matters for federal action is the pattern: when many owners of the same FORD ESCAPE cohort independently describe similar engine and engine cooling:engine:oil/lubrication: oil cooler failures, defect investigators have grounds to open a PE and request manufacturer data. Related filings for the same vehicle and component appear below, and the detail page for the full 2017 FORD ESCAPE shows the complete component-level complaint distribution alongside any active investigations or recalls.
Complaint Description
The contact owns a 2017 Ford Escape. The contact stated that while driving at 35 MPH, the vehicle inadvertently started jerking. There were no warning lights illuminated. The contact veered to the side of the road and opened the hood of the vehicle. The contact stated that he noticed that the vehicle did not have coolant and he refilled the coolant. The contact stated that as he continued to drive the vehicle, the vehicle started jerking significantly and was misfiring. The contact checked the engine coolant level and noticed that it was almost empty 15 minutes later. The contact stated that he added distilled water to the coolant reservoir. The contact stated that as he continued to drive that same day, the vehicle was jerking significantly. The contact turned off the vehicle and was unable to restart the vehicle without a jump start. The vehicle was towed to the contact's residence. The vehicle was then taken to the independent mechanic who diagnosed that the head gasket was fracture
Complaint Details
| NHTSA Complaint ID | 1780905 |
| ODI Number | 11442144 |
| Date Filed | November 30, 2021 |
| Failure Date | November 10, 2021 |
| VIN | 1FMCU0J98HU |
Source: NHTSA Vehicle Complaints Database. Component taxonomy and severity codes are standardized by NHTSA Office of Defects Investigation.
Read our methodology — how this data is sourced, computed, and verified.