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2018 BUICK ENCORE — Complaint #1770921

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NHTSA Complaint about ENGINE AND ENGINE COOLING:COOLING SYSTEM:HOSES/LINES/PIPING/FITTINGS filed September 29, 2021

NHTSA complaint #1770921 (ODI reference 11434883) concerns a 2018 BUICK ENCORE and was filed on September 29, 2021. The owner reports the failure occurred on July 29, 2021. The vehicle had 54,000 miles on the odometer at the time of the incident. The report was geocoded to Ohio based on the filer's self-reported location. The affected component is categorized as engine and engine cooling:cooling system:hoses/lines/piping/fittings, one of NHTSA's standardized taxonomy codes used to group defect patterns across make, model, and year.

The filer flagged the following severity indicators: crash: no, fire: no, injuries: 0, fatalities: 0. No crash, fire, or fatality was associated with this report, which places it in the early-warning stream rather than the priority-review stream. Because a VIN was supplied, this complaint is tied to a specific vehicle and not just a model-year cohort.

Individual complaints are consumer-submitted and unverified by NHTSA engineers — the agency's role at this stage is to collect, index, and make them searchable. What matters for federal action is the pattern: when many owners of the same BUICK ENCORE cohort independently describe similar engine and engine cooling:cooling system:hoses/lines/piping/fittings failures, defect investigators have grounds to open a PE and request manufacturer data. Related filings for the same vehicle and component appear below, and the detail page for the full 2018 BUICK ENCORE shows the complete component-level complaint distribution alongside any active investigations or recalls.

Vehicle
2018 BUICK ENCORE
Component
ENGINE AND ENGINE COOLING:COOLING SYSTEM:HOSES/LINES/PIPING/FITTINGS
State
Ohio
Mileage
54,000 mi

Complaint Description

The contact owns a 2018 Buick Encore. The contact stated while driving at various speeds, the check engine warning light would illuminate as the average miles per gallon decreased. The vehicle was taken to the dealer who stated that the clamps for the turbo hoses were loose. The clamps and hoses were realigned and tightened. The contact stated that the failure recurred 2 months later. The vehicle was taken back to the dealer and the same diagnosis along with a red thread failure. The clamps were realigned and tightened again. The contact stated that the air filter hose was also loose. The manufacturer was not made aware of the failure. The approximate failure mileage was 54,000.

Complaint Details

NHTSA Complaint ID 1770921
ODI Number 11434883
Date Filed September 29, 2021
Failure Date July 29, 2021
VIN KL4CJASB1JB

Source: NHTSA Vehicle Complaints Database. Component taxonomy and severity codes are standardized by NHTSA Office of Defects Investigation.